
Hi Pali,
On Fri, Feb 10, 2023 at 1:44 PM Pali Rohár pali@kernel.org wrote:
On Friday 10 February 2023 13:38:44 Tony Dinh wrote:
Hi Stefan, Hi Pali,
On Fri, Feb 10, 2023 at 9:29 AM Pali Rohár pali@kernel.org wrote:
On Thursday 09 February 2023 17:37:54 Tony Dinh wrote:
Hi Pali,
On Thu, Feb 9, 2023 at 1:45 PM Pali Rohár pali@kernel.org wrote:
On Thursday 09 February 2023 13:33:23 Tony Dinh wrote:
Hi Stefan,
On Wed, Feb 8, 2023 at 11:15 PM Stefan Roese sr@denx.de wrote: > > Hi Tony, > > On 2/9/23 04:17, Tony Dinh wrote: > > Hi Stefan, > > > > On Fri, Feb 3, 2023 at 4:11 PM Tony Dinh mibodhi@gmail.com wrote: > >> > >> Hi Pali, > >> > >> On Fri, Feb 3, 2023 at 2:05 PM Pali Rohár pali@kernel.org wrote: > >>> > >>> On Thursday 02 February 2023 19:04:45 Pali Rohár wrote: > >>>> On Wednesday 01 February 2023 13:13:16 Tony Dinh wrote: > >>>>> Hi all, > >>>>> > >>>>> On Wed, Feb 1, 2023 at 11:05 AM Pali Rohár pali@kernel.org wrote: > >>>>>> > >>>>>> On Wednesday 01 February 2023 09:17:15 Michael Walle wrote: > >>>>>>>>>> When DM_SERIAL is enabled, the device-tree property dm-pre-reloc is > >>>>>>>>>> required to boot over UART with kwboot. Enable this in a Kirkwood > >>>>>>>>>> common u-boot dtsi. > >>>>>>>>> > >>>>>>>>> My (dev) board unfortunately, have a bootloader which can't boot over > >>>>>>>>> serial. > >>>>>>>> > >>>>>>>> This is feature of Marvell BootROM and does not require any special from > >>>>>>>> Bootloader. So you should be able to boot over UART (if you have > >>>>>>>> accessible pins). > >>>>>>> > >>>>>>> I know, but there are known versions ob the bootrom where uart boot > >>>>>>> isn't supported (correctly). > >>>>>> > >>>>>> I heard about it... maybe it is a bug in client software (kwboot)? I do > >>>>>> not have such board if you are interested in it I could try to send some > >>>>>> details how to debug it. > >>>>> > >>>>> The Kirkwood SoCs came with different BootROM versions. Version 1.1 > >>>>> cannot be booted over UART, but version 1.2 can. I think there must > >>>>> be a bug in the BootROM 1.1. The older Kirkwood such as Sheevaplug, > >>>>> Dockstar, iConnect boards come with BootROM 1.1. Later version of > >>>>> Sheevaplug, GoFlex Home, GoFlex Net, Dreamplug, Pogoplug V4, Zyxel > >>>>> NSA310S, NSA320, NSA325 come with BootROM 1.2. So even though it is > >>>>> the same SoC, eg. 6281, they are actually produced at a different time > >>>>> and have different BootROM versions. > >>>> > >>>> There are always multiple revisions of the same SoC. So it is possible > >>>> that something was broken on first revision of 88F6281 and in next > >>>> revision was updated BootROM with some fixes. Revision is written on > >>>> package label and for Armada SoCs it is available also in some register > >>>> (not sure about Kirkwood). It looks like that there is at least revision > >>>> Z0 and revision A0 of some Kirkwood SoC. > >>>> > >>>> If there is a bug in first revisions then it should be documented in > >>>> some Kirkwood Errata document. Unfortunately I have never seen it, it is > >>>> not public, so I have no idea. In any case, if somebody has access to > >>>> Marvell documents, interesting are these document numbers: > >>>> > >>>> * MV-S105223-001 - Differences Between the 88F6192, and 88F6281 Stepping Z0 and A0 > >>>> * MV-S501081-00 - 88F6180, 88F6192, and 88F6281 Functional Errata, Interface Guidelines, and Restrictions > >>>> * MV-S501157-U0 - 88F6180, 88F6190, 88F6192, and 88F6281 Functional Errata, Interface Guidelines, and Restrictions > >>>> > >>>> One of the option how to investigate or debug this issue without > >>>> documentation is to dump both BootROM versions (1.1, 1.2) and compare > >>>> them. Either there is different UART protocol for booting (which needs > >>>> to be implemented) or UART protocol is buggy and needs some workaround > >>>> or it is completely broken and does not work. > >>> > >>> BootROM is mapped to 0xF8000000 address and is 64 kB long. So via U-Boot > >>> md command it is possible to dump it over console. Or via ext4write > >>> command store it so ext4 fs on sd card / sata disk. > >> > >> Thanks for the info. It will be a while before I can get back to this > >> BootROM 1.1 vs 1.2 topic. > >> > > > > I have run some more tests, and am quite positive that if the uart0 > > node exists in the DTS, it must be tagged with dm,pre-reloc. That is > > consistent with the serial documentation in > > doc/develop/driver-model/serial-howto.rst. The issue is whether the > > uart0 node is specified in the DTS. If it is, the dm-pre-reloc tag > > must also be used. > > > > To prove my theory, I've modified the Pogo V4 DTS to look exactly like > > the NSA310S, as far as uart0 is concerned. The NSA310S does not even > > have a uart0 node! and DM_SERIAL boots fine with this box. With the > > patch below, the Pogo V4 can be kwboot and run normally. No > > dm-pre-reloc tag is needed. > > > > diff --git a/arch/arm/dts/kirkwood-pogoplug-series-4.dts > > b/arch/arm/dts/kirkwood-pogoplug-series-4.dts > > index 5aa4669ae2..227d5ff802 100644 > > --- a/arch/arm/dts/kirkwood-pogoplug-series-4.dts > > +++ b/arch/arm/dts/kirkwood-pogoplug-series-4.dts > > @@ -24,7 +24,8 @@ > > }; > > > > chosen { > > - stdout-path = "uart0:115200n8"; > > + bootargs = "console=ttyS0,115200"; > > + stdout-path = &uart0; > > }; > > > > gpio_keys { > > @@ -97,10 +98,6 @@ > > }; > > }; > > > > -&uart0 { > > - status = "okay"; > > -}; > > - > > /* > > * This PCIE controller has a USB 3.0 XHCI controller at 1,0 > > */ > > FWIU, you are hitting a bug in the early serial console code, perhaps > in serial_check_stdout()?
Quite possible. But I recall trying the same stdout path as the NSA310S, i.e. stdout-path = &uart0. So the stdout-path itself is not the reason. Perhaps the bug is in another part of the function.
> > Could you please check if Pogo V4 boots with > CONFIG_REQUIRE_SERIAL_CONSOLE unset? > Indeed, you're right! unset CONFIG_REQUIRE_SERIAL_CONSOLE allows the Pogo V4 to boot OK, without dm-pre-reloc needed. And it booted normally with kwboot, all serial input/outputs are OK.
> > Also, note that just enabling DEBUG_UART would always make the board > > frozen when u-boot starts. > > This should not be the case of course. Are you sure you've correctly > configured the DEBUG UART?
I think I did that correctly (we've used that to debug the orion_timer issue previously). Here is how I've configured it:
+CONFIG_DEBUG_UART_BASE=0xf1012000 +CONFIG_DEBUG_UART_CLOCK=250000000 +CONFIG_DEBUG_UART=y
Maybe you hit same issue in mach-kirkwood as me in the past for mach-mvebu? U-Boot code was trying to initialize UART at the _new_ base register address (0xf1012000) when U-Boot was still using the _old_ base register address (0xd0012000).
I fixed it by moving code which changes base register address from arch_cpu_init() function to arch_very_early_init() function in commit: https://source.denx.de/u-boot/u-boot/-/commit/5bb2c550b11eb087437740b2a0d1fe...
Thanks for the info! Looking at that patch, I think I'm out of my depth :)
That is pretty simple. It is something like this:
diff --git a/arch/arm/mach-kirkwood/Kconfig b/arch/arm/mach-kirkwood/Kconfig index c8a193dd4cdf..ba39e9ae416e 100644 --- a/arch/arm/mach-kirkwood/Kconfig +++ b/arch/arm/mach-kirkwood/Kconfig @@ -5,9 +5,11 @@ config FEROCEON_88FR131
config KW88F6192 bool
select ARCH_VERY_EARLY_INIT
config KW88F6281 bool
select ARCH_VERY_EARLY_INIT
config SHEEVA_88SV131 bool diff --git a/arch/arm/mach-kirkwood/Makefile b/arch/arm/mach-kirkwood/Makefile index 3b2eef8d5419..0fb5a2326f5f 100644 --- a/arch/arm/mach-kirkwood/Makefile +++ b/arch/arm/mach-kirkwood/Makefile @@ -6,6 +6,7 @@
obj-y = cpu.o obj-y += cache.o +obj-y += lowlevel.o obj-y += mpp.o
# cpu.o and cache.o contain CP15 instructions which cannot be run in diff --git a/arch/arm/mach-kirkwood/cpu.c b/arch/arm/mach-kirkwood/cpu.c index df3e8f11782a..2b493b36c20d 100644 --- a/arch/arm/mach-kirkwood/cpu.c +++ b/arch/arm/mach-kirkwood/cpu.c @@ -189,9 +189,6 @@ int arch_cpu_init(void) struct kwcpu_registers *cpureg = (struct kwcpu_registers *)KW_CPU_REG_BASE;
/* Linux expects the internal registers to be at 0xf1000000 */
writel(KW_REGS_PHY_BASE, KW_OFFSET_REG);
/* Enable and invalidate L2 cache in write through mode */ writel(readl(&cpureg->l2_cfg) | 0x18, &cpureg->l2_cfg); invalidate_l2_cache();
diff --git a/arch/arm/mach-kirkwood/lowlevel.S b/arch/arm/mach-kirkwood/lowlevel.S index e69de29bb2d1..3b339f97f056 100644 --- a/arch/arm/mach-kirkwood/lowlevel.S +++ b/arch/arm/mach-kirkwood/lowlevel.S @@ -0,0 +1,12 @@ +/* SPDX-License-Identifier: GPL-2.0+ */
+#include <config.h> +#include <linux/linkage.h>
+ENTRY(arch_very_early_init)
/* Move internal registers from KW_OFFSET_REG to KW_REGS_PHY_BASE */
ldr r0, =KW_REGS_PHY_BASE
ldr r1, =KW_OFFSET_REG
str r0, [r1]
bx lr
+ENDPROC(arch_very_early_init)
Thanks! I'll try this eventually. But please see my response to Stefan below. Would the forced setting CONFIG_DEBUG_UART_BASE=0xd0012000 give us some output from uart0 before arch_early_init ?
I do not know if it gives us any output. It depends on when u-boot start printing something on UART. Beware that initialization of UART can be more earlier than printing something. Note that after arch_cpu_init() is 0xd0012000 invalid. So if initialization happens before arch_cpu_init() but printing starts after arch_cpu_init() then nothing would be visible and it will always fail.
For now I will fix this Pogo V4 with the -u-boot.dtsi, so as not to mess up anybody who might try UART booting with kwboot.
Thanks, Tony
> > So this was another factor why it took me > > so long to figure this out :) I've just restored everything and > > removed the uart0 node from the Pogo V4 DTS like above and it is > > working. > > > > But of course, we don't want to change the Pogo V4 DTS, so I will > > submit another patch just for the Pogo V4 to add -u-boot.dtsi for this > > box to enable the dm-pre-reloc tag for uart0. > > Understood.
Regarding Stefan's suggestion about trying using CONFIG_DEBUG_UART_BASE=0xd0012000. Yes, I also tried that address (I'm aware of this address while building kernels for some old Armada 370 boards such as the Mirabox and Netgear RN102). I suspect for some reason, i.e. bug, at the pre-relocation phase we don't even have the uart0 device so DEBUG UART printch() just hangs.
Thanks, Tony
DEBUG UART does not use DM / DT devices like uart0. DEBUG UART does not use DTS file. So even with broken DTS file DEBUG UART should work fine.
Sorry, I meant the serial device that DEBUG UART uses, not the specific uart0! I think that device does not exist at that point.
Anyway, I tried your patch for ARCH_VERY_EARLY_INIT, and the behavior is the same. Subsequently, with this patch I also tried taking out all printch() calls (to make sure nothing is output). The board is just frozen right when u-boot starts.
I think I'll let this problem stew for a while, and come back later. I will turn off DM_SERIAL and run some tests then.
In the meantime, if anybody has any Marvell SoC defconfig in which DEBUG_UART was working with DM_SERIAL, I'd appreciate it if you can send that defconfig.
Thanks, Tony